Return-Path: Received: from smtp108.mail.sc5.yahoo.com ([66.163.170.6] verified) by logan.com (CommuniGate Pro SMTP 4.2.5) with SMTP id 555782 for flyrotary@lancaironline.net; Sat, 04 Dec 2004 09:23:47 -0500 Received-SPF: none receiver=logan.com; client-ip=66.163.170.6; envelope-from=prvt_pilot@yahoo.com Received: from unknown (HELO stevehome) (prvt?pilot@24.136.229.34 with login) by smtp108.mail.sc5.yahoo.com with SMTP; 4 Dec 2004 14:23:14 -0000 Reply-To: From: "Steve Brooks" To: "'Rotary motors in aircraft'" Subject: power sag Date: Sat, 4 Dec 2004 09:23:08 -0500 Message-ID: <000101c4da0c$c7806640$6b01a8c0@workgroup.com> MIME-Version: 1.0 Content-Type: text/plain; charset="iso-8859-1" Content-Transfer-Encoding: 7bit X-Priority: 3 (Normal) X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook CWS, Build 9.0.6604 (9.0.2911.0) Importance: Normal X-MimeOLE: Produced By Microsoft MimeOLE V6.00.2800.1441 I went to South Carolina Thursday to replace the fuel regulator, and do some flying. I replaced the regulator, and ran the engine some on Thursday, but no flying because it was getting dark. On Saturday, I went to fly, and had some trouble getting it to stay running due to the cold temperatures. I probably didn't keep it rich enough, long enough. I taxied out to the far end of the runway (5000'), and took the runway for take off. As I accelerated to about 90 kts, I was just rotating when to power dropped substantially. I cut the throttle, and aborted the takeoff. I don't know exactly what caused the sag. I pulled the throttle all the way back during the aborted takeoff, and the engine died. I have my idle stop set a little low (400 RPM's), and usually don't pull it all the way off, but even when I do, it has never died. I restarted it, and ran the power up to about 4000, and it seemed OK. Another issue with my right main wheel bearing prevented me from making any more high speed runs. The right wheel has been making noise, and I was trying to resolve it with the mfg, but during the aborted take off, it really made allot of noise, and also vibrated pretty good at one speed, so I decided that I better get that fixed before doing any more flying. I changed the fuel regulator, so I guess that it could have been some air still in the fuel line, but the engine had probably run for at least 10 minutes prior to the take off roll. It also could have been some water, though I've never found any to date during preflight. The engine was running at 5 lbs of boost and about 5000 RPM's. It was about 45 degrees, and the plane was accelerating very strong prior to the power loss. I don't know if it would have picked back up, but I was glad that it didn't happen 5 seconds later. Steve Brooks