Return-Path: Received: from web51103.mail.yahoo.com ([206.190.38.145] verified) by logan.com (CommuniGate Pro SMTP 4.2.5) with SMTP id 546754 for flyrotary@lancaironline.net; Fri, 26 Nov 2004 16:59:17 -0500 Received-SPF: none receiver=logan.com; client-ip=206.190.38.145; envelope-from=prvt_pilot@yahoo.com Received: (qmail 21645 invoked by uid 60001); 26 Nov 2004 21:58:46 -0000 Comment: DomainKeys? See http://antispam.yahoo.com/domainkeys DomainKey-Signature: a=rsa-sha1; q=dns; c=nofws; s=s1024; d=yahoo.com; b=JP+Ov333h98TCkzDr9jPaCxYoSjD8SlMTRD9i5IhXZr1u4qIzFieoBE8amIrh6DZLJwK/962Sz1/zLyivIH4l8I/e60EOFomgg6XLwFFcTELwwWo2vLXYvtnOMoCKOurnF/lxi5x1tutiJVLFaxBvqhGq+xrmlCdgGZlcwdH3UA= ; Message-ID: <20041126215845.21643.qmail@web51103.mail.yahoo.com> Received: from [12.146.251.241] by web51103.mail.yahoo.com via HTTP; Fri, 26 Nov 2004 13:58:45 PST Date: Fri, 26 Nov 2004 13:58:45 -0800 (PST) From: Steve Brooks Subject: Great first flight today - but sadly no second flight To: flyrotary@lancaironline.net MIME-Version: 1.0 Content-Type: text/plain; charset=us-ascii I intended to fly several hours on Friday and Saturday, and had a great first flight of about 1/2 hour. The OAT was 50 degrees, and the engine temperatures were fantastic due to the mods, and the cooler temperatures. The oil never went above 160, and the coolant never went above 180. the engine was running good (aside from one issue), and the plane was flying great. When I throttled back, I noticed some roughness in the engine, and after fiddling with the mixture a little, I realized that I had left the 2nd EFI pump on. As soon as I shut off the 2nd pump, the engine smoothed right out, and there were no further issues. I tested the two pump issue once on the ground, but at low power, it seemed to make no difference. I checked the plane over for any oil leaks, parts dangling, wings falling off, etc., and all look OK. I went to lunch, and got more fuel, so that I could fly for at least another hour. I fueled up, and taxied out to runway 9 at the far end of the airport. About a 1 mile taxi. When I got to the run-up spot, I went through the check list, and went to adjust the mixture to a richer setting for takeoff. When I looked at the air ratio gauge, it was off the scale rich, with the mixture knob set at 12 o'clock. I ran the mixture all the way CCW to lean, and instead of dying, like it usually does, it only turned off the top LED on the A/R gauge. After going back to the hanger, I discovered that I didn't have my fuel pressure gauge with me, but I did have a 0-80 lb. sender, that I had planned on installing for when I add the EM2 (someday). I installed the sender, and turned on the fuel pump. It read about 90 ohms. The sender is a 10-180 ohm sender. If it's linear (don't know that it is), then it should be about 45 lbs or so of pressure. I turned the fuel regulator down to 80 ohms, and started it. No difference. After adjusting down about 10 ohms at a time, it finally ran better at about 40 ohms. While watching the ohm meter, I kicked on the 2nd fuel pump, and the resistance went from 30 ohms to 90 ohms. Not too good. Looks like I'm going to need a new fuel regulator. The one I have now is a Mallory 3 port (return style), but I think that I'll buy something other than Mallory, since this one failed so soon. Can someone recommend a 3 port regulator that is working well for them ? I remember reading about this subject a couple of months ago, but I'm not at home, and can't find the link to the archive search. Thanks, Steve Brooks (at least my turbo still works) Cozy MK IV Turbo Rotary