Mailing List lml@lancaironline.net Message #69994
From: Chris Zavatson <chris_zavatson@yahoo.com>
Sender: <marv@lancaironline.net>
Subject: Re: [LML] Cooler CHTs
Date: Tue, 13 May 2014 07:45:06 -0400
To: <lml@lancaironline.net>
Bill,
Is that a new engine? -looks spotless.
Scott Krueger was also able to get a really good seal on his baffles.  In fact, he had the highest measured pressure recovery I have seen using flexible baffle material.  You wouldn't happen to have (or be interested in measuring) some upper plenum pressures for comparison?  -forever in search of cooling system data.
How do you interface to the inlets? -any pics of that area?
thanks,
Chris Zavatson
N91CZ
360std
www.N91CZ.net
On Monday, May 12, 2014 4:46 AM, William Rumburg <lancair403@verizon.net> wrote:
I maintain that the conventional baffling structure, which has a well-executed flexible seal at the upper cowl and a form-fitting seal at the cooling air inlets, can be almost as effective as a plenum. The gap to the upper cowl must be uniform, not less than 3/4 inch or much greater than 1 inch. It should, ideally, be 1 inch all around. My Lancair-supplied baffling had too much gap at the right rear cowl, and too little at the left rear, because the engine is slightly rotated with respect to the cowl. In addition, a major shortcoming of the Lancair-supplied baffling is that it leaves a WIDE gap at the cooling air inlets, with builders doing little more than adding some loosely-fitting, ineffective seal there. It wasn't too difficult to correct both of these conditions and add some other enhancements, which resulting in lowering my cruising CHT's by 40 degrees, from 360-380 to 320-340.
As seen in the photos, I added a 1 inch wide aluminum strip across the front, easily cut from a cardboard template. That not only transformed the baffling into a rectangular box, making it easier to seal, but allowed for the addition of custom fiberglass seals at the air inlets. I formed those by trimming a block of foam to the required shape and overlaying with duct tape for release. Their circular holes match the air inlets, with only 1/8 inch gap to the cowl. In addition, I re-cut both of baffling side pieces to their correct heights, utilizing .050 inch thick aluminum, and made custom 1 inch-high inner pieces -also easily cut from cardboard templates- so as to 'sandwich' the flex seals, further decreasing air leakage. I carefully cut all seals to the correct height and shape and feel that I've obtained a nearly 100% seal. I also reduced airflow wasted through engine areas other than the cylinder heads.
 
Bill Rumburg
N403WR (Sonic bOOm)

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