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Posted for <n98pb@sbcglobal.net>:
First, I am writing this after reviewing all the information provided by the
NTSB and the LML list. The plane Dave was flying lifted off Somerset, PA,
at treetop height it started emitting heavy black smoke and the engine
sputtered and stopped producing power.
Last week in Corona, CA I had an event that didn't strike me as relative
until I reread those documents. N98PB, IVP with 650 hours and just
completing a 25 hour trip to East Coast Destinations. During that trip I
noticed that my normal Lean of Peak condition at 16.5 GPH was running rough
until I increased it to about 17GPH where it settled down. A LOP mag check
was done at both fuel flow settings and at 16.5 it ran rough on both, at 17
it was smooth on each of the mags. I attributed this to a clogged injector
and cleaned them upon returning home. Temps during the trip all remained
within the engines normal parameters.
Now the issue: I cleaned the injectors, pulled and cleaned the gascolator
screen and blew out all the injector lines to the spider. After this I did
a full run-up and took to the air. On the ground the run-up was uneventful.
This changed once I left the ground. Heavy black smoke and a very rough
engine occurred just after lift off at about 100 feet or so. I pulled the
throttle back about 5 inches to just over 30, the engine smoothed out some
and ground reports indicated that the smoking had ceased. I realized the
engine was going to continue running and turned back to the runway with a
shallow 180. I continued over the runway and again made a 180 for a normal
landing into the wind. Once on the ground the plane was de-cowled and
inspected by a number of knowledgeable A/P types. Again the injectors were
inspected and cleaned, the valve covers removed to assure all rocker bosses
and valves were acting normally through rotation and the gascolator removed
and inspected. All appeared normal. I taxied the plane to the run-up area
and did a high power run-up with all indications normal. Two high speed
taxi tests were done and everything appeared normal. I lined up and took
off again. Same result ground run was perfect with the exception of
slightly lower RPM (2650), rough engine once airborne, black exhaust, a
check of the engine parameters indicated a full throttle fuel flow of 47.5
gallons an hour(ff is set for 45.5 gph). A pull back to 30 inches stopped
the black exhaust and the engine ran much smoother. An uneventful landing
and another disassembly. The fuel pump was sent to a shop for inspection
and found to have a sticking aneroid and I am awaiting its return. I also
found several cracks in the right exhaust Tee which I don't think is related
to the engine roughness and high fuel flow issue but is going to be a
frequent inspection item as it could have been catastrophic.
I don't know how of if this could relate to Dave's accident but it appeared
so similar I wanted to put it out for thoughts and reference. I won't have
an positive answer to the issue until the parts are back and installed for a
flight test but the pump is certainly outside of parameters.
Comments and thoughts welcomed.
Pat Brunner
N98PB 650 hours IVP
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