Return-Path: Sender: (Marvin Kaye) To: lml Date: Wed, 30 Oct 2002 19:49:00 -0500 Message-ID: X-Original-Return-Path: Received: from smtprelay6.dc2.adelphia.net ([64.8.50.38] verified) by logan.com (CommuniGate Pro SMTP 4.0) with ESMTP id 1848816 for lml@lancaironline.net; Wed, 30 Oct 2002 17:26:05 -0500 Received: from library ([216.227.164.122]) by smtprelay6.dc2.adelphia.net (Netscape Messaging Server 4.15 smtprelay6 Dec 7 2001 09:58:59) with SMTP id H4TFNF00.CI2 for ; Wed, 30 Oct 2002 17:26:03 -0500 X-Original-Message-ID: <003301c28063$53d6d120$7aa4e3d8@library> From: "Doug Pohl" X-Original-To: "Lancair Mailing List" Subject: Engine Power Systems Preliminary Report on the Duke Accident X-Original-Date: Wed, 30 Oct 2002 17:25:52 -0500 MIME-Version: 1.0 Content-Type: text/plain; charset="iso-8859-1" Content-Transfer-Encoding: 7bit X-Priority: 3 X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook Express 6.00.2800.1106 X-MimeOLE: Produced By Microsoft MimeOLE V6.00.2800.1106 10/30/02 The following is an unofficial announcement of Engine Power Systems LLC preliminary report on the Beech Duke crash of 10/20/02. This information is based upon discussions with FAA and NTSB investigators, local sheriff and a paramedic that was first on the crash site as well as other witnesses knowledgeable in the events described. A 427 cubic inch 500 HP V-8 engine application was developed by Engine Power Systems LLC over the past year and installed on a 1973 Beech Duke. An Experimental Exhibition type certificate was issued by the FAA for the plane in September of this year. The type certificate contained no flight limitations and permitted IFR and night flight with no flight test requirements. Following the minimal first flight tests in Florida, the plane was flown over 1,100 nautical miles by the owner and displayed at the Duke Owner's Association convention at Sault St. Marie Canada last month. Due to time constraints of the annual Duke Owner's Association show, there is no evidence at present that a systematic flight test program was conducted by the owner or that all instrumentation crucial to the operation of the plane and its engine was completed prior to the fatal flight. It should be understood that the Duke engine application was a complex project involving a 24-volt airframe and a 12-volt engine system. The owner of the Duke and copilot departed Sault St. Marie several days prior to the crash en-route for autopilot and panel work in Muncie, Indiana. Following engine shutdown, attempts to restart the right engine revealed a dead battery. There was an apparent problem with the 12 volt charging system on the right side engine and a battery charger was placed on the battery and a restart successfully made. Besides work being done on the autopilot, the details of the specific panel work performed are not yet available. The work required several days, delaying the pilot's departure to Florida. The pilot was scheduled to return to Canada on Thursday, 10/21/02 by scheduled airlines. The pilot had a meeting scheduled in Florida on the night of departure with a fellow Duke owner. The purpose of the meeting was to provide new capital to Engine Power Systems LLC to fund certification of the engine package. The engine installation included a 12-volt alternator on the starboard engine and 24 volt alternator on the port engine. The Duke was equipped with standard instrumentation to monitor the 24-volt alternator system, however no such instrumentation had yet been installed for monitoring the 12-volt alternator system. It was the impression of the avionics specialist that the starboard 12-volt alternator system was not functioning properly. On the night of departure, the pilot was advised of the problem and advised not to depart. Additionally, the instrument panel lights were not functional, necessitating the use of external (flashlight) lighting. Despite the known electrical problem and lack of instrument lights, the pilot elected to depart. Departure occurred in rain and at night under an IFR flight plan with known worsening conditions to the south for a minimum 4 hour flight to Melbourne, Florida. The flight proceeded uneventfully for approximately 2 1/2 hours at which time there was an apparent total loss of power to the right engine. Calculation of the battery capacity and electrical consumption of the right side engine computer indicates that the engine would have run faithfully for approximately 2 hours until the voltage fell below 9 volts, at which time the engine electrical systems would shut down leading to loss of the engine running. The pilot reported his problem to ATC and requested diversion to the nearest airport at Jesup, Georgia. According to witnesses on the field, conditions at Jesup, Georgia were 1000 foot ceiling. The field had no ILS approach and it appears that the approach to the field was made using an NDB/GPS approach. The pilot reported to ATC that he had the field in sight after breaking out of the overcast at 1000 feet. The plane apparently was not aligned with the runway and it is assumed that the pilot had attempted to go around to align the plane for landing. The starboard engine prop was feathered, the wheels were down and possibly the flaps were down as well (most of the wings were consumed in the fire) indicating that full power was applied to the left engine to slow descent and maneuver for landing. One of the assumptions being made is that the pilot never practiced single engine flight with the new engine configuration and possibly underestimated the additional 120 HP produced by the left engine thus causing the plane to yaw, digging in the right wing, spinning the plane and impacting the ground. The pilot and co-pilot perished and were consumed in the ensuing fire. Official cause of Accident: Pending final report of the NTSB.