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I did switch power sources, but flying the airplane distracted me from switching controllers. As for the coils, I could test them, but what are the chances of all four going bad at the same instant??
The controller will be going to Tracy for analysis.
Bill
On Sat, Sep 3, 2011 at 8:30 AM, Finn Lassen <finn.lassen@verizon.net> wrote:
I suppose you did not have time to switch over to the B controller?
Any way of testing the ignition coils?
Finn
On 9/2/2011 11:51 PM, Bill Eslick wrote:
I have
been holding up reporting this until all the facts are in, but
that might never happen, so here we go.
Good news: No injuries.
Bad news: I have some work to do.
Photos at: http://www.tiny9.com/u/2101
On August 16th at 10 AM, I lined up for takeoff at my home
airport (3600' paved) into a 5 knot headwind. I had just
finished changing the oil and filter and plugs. Run-up was
fine, so off I went. Approximately mid-field, and a couple
of hundred feet in the air, it suddenly and without any
warning became very silent.
Hit the big switch which puts direct battery power to
everything engine, but no noise. No more time. At this
point flying the machine becomes THE priority. Dropped the
nose and was amazed to see a little bit of runway under the
nose! I had fully expected to land in trees, houses or the
river, so I dove what seemed like straight down to capture
as much runway as possible while (somehow) holding the
electric flap switch long enough to get full flaps (noticed
this later). Pulled probably my best round-out ever - no
bounce. Brakes to max and tail up for weight. I think my
sub-concious put it all the way on the nose to try to
prevent going through the fence and down the hill. Wheel
skid starts about 200 feet from the stopping point. Skid
marks from the wheel pants, cowling and prop run about the
last 50 feet. It stopped nose down just off the end. The
tail was still over pavement. Pushed the slider canopy
UPHILL, stepped out and down. Noticed that I was not even
scared by the whole event. Interesting. Never even
considered trying to turn around. Pre-thinking that
non-option apparently paid off.
More good news. No FAA or NTSB as it was a non-reportable
incident. Didn't even bend the gear legs. Also, my
neighbor crashed in a Challenger about 10 minutes earlier at
the city airport about 10 miles away. The police and rescue
types were headed that way (they had injuries) and were not
interested in my minor mishap.
As for the engine. When we got it back to the hangar, the
prop would turn only haltingly. You could feel grinding
going on inside. First try at turning had it come up hard
and stop. More fooling with it and it gradually came looser
and would turn. Really looked like something came loose in
there. Pulled a plug from each rotor and did a compression
test. Rotor 1 was 80-80-80. Rotor 2 was 2-2-2. More proof
that something had come loose. With that evidence, the
insurance company allowed me to remove the engine for
inspection. What I found was a pile of ground up ceramic
junk. All the seals were still fine. Lots of time went in
to finding where that stuff came from. Went through every
inch of the induction system. Finally Jason Hutchison (my
other on-airport rotary guy) broke the code. While the RV
was standing on it's nose, this crap from my burned-out
Hushpower II ran back up the manifold and in the exhaust
port. That is what was grinding. Crap. Now the entire
thing is off the firewall including the engine mount. All
the wiring is disconnected (did not find anything loose or
missing). I spent the morning looking under the panel for
any loose or broken wiring, but found none. When I get the
EC-2 out, Jason wants to plug it into his plane and we'll do
the plugs and injectors test. If that checks out, Tracy, it
is coming to you for a good look. I don't know what else to
check. The engine quit just like somebody reached over and
turned off the ignition. No stumble, no hiccup, just
instant silence. I honestly do not know if the prop was
turning or not. I suspect not, due to the silence and the
fact that one blade is untouched.
As you can see from the photos, there was something going on
with Rotor 1. Wear is apparent down stream from the plug
holes and all 3 apex seals are starting to chip in the
center. There is quite a lot of carbon also on the rotors
after 170 hours.
Going forward, I have decided to look at resale value for
if/when my RV-12 days arrive. This means putting a (gasp)
IO-360 on it. The rotary has given me a safe 10-year run
(til now, of course), so I have no regrets, but this is an
opportunity to make some changes, and parts are already on
the way. I will still be hanging out at the engine tent at
S-n-F and wherever else gatherings happen. Hope to be
flying by the first of next year....
I'm sure some of you will have suggestions about what might
have gone wrong, and I welcome any kind of speculation, but
bear in mind I am just looking at a pile of parts and wires
at this point. Both fuel pumps were on, tanks were over
half full, crank angle sensor worked fine.
Guess it's obvious that I now have a RD-1A, EC-2, EFI
Monitor (Ed's), Felix 68/72 and Props Inc 68/72 wood props
and LOTS of engine parts (my whole 14-year stash)
available! And priced to sell!
Bill Eslick
RV-6 13B/NA EC-2 RD-1A
750 Hours
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