Mailing List flyrotary@lancaironline.net Message #45381
From: Jim Perdue <guinnessguy74@yahoo.com>
Subject: Ground Testing
Date: Sun, 8 Mar 2009 19:50:07 -0700 (PDT)
To: Rotary motors in aircraft <flyrotary@lancaironline.net>
Hello everyone. I've been reading this mailing list for a bit, and I am very impressed with the knowledge and experiences being shared here. It is everyone here who is paving the way for the rotary installations of the future. I for one am very grateful.
 
I am currently building a Cozy MKIV and I am seriously considering a rotary. Most likely a renesis, but possibly considering a 20B. I have rebuilt a few engines in my day (piston of course). I am far from needing an engine, but I was wondering if some of you can answer a question? I realize there are in-flight challenges that can only be addressed at that time of course, but how much can you debug/learn from ground testing an engine? Can anyone tell me what can be acheived during ground testing and what cannot? Even though I am far away from a powerplant, I'd like to pick up a cheap engine and start "playing" ;-)
 
I appreciate any input on this subject. Thanks!
 
Jim
Charlotte, NC


From: Mark Steitle <msteitle@gmail.com>
To: Rotary motors in aircraft <flyrotary@lancaironline.net>
Sent: Sunday, March 8, 2009 9:18:55 PM
Subject: [FlyRotary] Re: I've got oil pressure!

That's great news Chris.  Glad you figured out the problem. 

Mark S.

On Sun, Mar 8, 2009 at 7:23 PM, The Mallorys <candtmallory@cebridge.net> wrote:

I made some good progress this weekend.  After trying to prime the oil pump and still not getting any oil flow, I broke down and removed the pan.  There was the culprit, big as day.  I had a kink in the oil pickup line.  Because I am installing an inverted oil system, I have to run the line from the pump back out the pan to the inverted oil ball valve.  This line needed a bend, and I thought the hose could handle it, but I was wrong.  SO I replaced the bend with metal parts, and reassembled everything.  Now I’ve got 60 PSI.  I also burped the coolant, and that system seems to be working too.

 

I did find a couple of leaks that will have to be fixed, but that is all minor work.

 

Thanks all for the helpful words!

 

Getting closer every day.

 

Chris



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