Everyone has a view point concerning
cooling (at least one {:>)). Once you get a high performance aircraft
fairly clean drag-wise the largest remaining drag is generally the cooling
system.
Ideally, you choose some regime of flight
to optimize your cooling system for. A bush pilot might opt to optimize
for slow and low and high power settings. A high altitude cruise type
might optimize the cooling system for that regime. Which ever you do its
always a compromise of various factors.
In the many experiments with my ducting
system over the past 10 years, I believe I have arrived at (for me)
fairly close to the optimum. The reason I draw this conclusion is that at
7500 MSL and max throttle (12-14 GPH fuel flow) my cooling and oil temps
increase until they are less than 5 deg below my max desired temps (200F for
both). Any more power and I would encounter a cooling deficit - any more
cooling and I will be carrying more drag than necessary. Now, while I do
believe I am close to the optimum for my prefer operating conditions, I do
acknowledge that there is a price to pay on the low end.
From take off roll until attaining an
airspeed of 120 MPH IAS I run a cooling deficit and my coolant may hit 210-220F
and oil 200F for those few minutes. After hitting 120, I start to catch
up on temperature curve and generally within 5 minutes things are stabilized
around 170-185 deg for both. I fly without a thermostat and as a
consequence can see much lower temps in cruise. In fact coming home from
the Rotary Round up with OAT showing 53F and burning 8 gph my temps were below
160F.
My total radiator intake area is 36 sq
inch with another 22 sq inch for the oil cooler. My exit opening is
rather large and I undoubtedly get a bit of drag with it – around 80 sq
inches plus louvers along both sides of the cowl.
I could only do a 7 gph ground run
up on a 70 F day for approx 2-3 minutes before temps start getting close to
200F. I can taxi all day without any problem on temps.
Here are three photos that may be of
interest. The finsCowl.jpg was my standard intake for many years and
while it cooled fine, I felt it had more drag than necessary. After quite
a bit of research I developed what I call my “Pinched ducts”
reducing the opening and inducing a bell flair similar to the “StreamLine
Duct”. This reduced the area of the opening considerably and
coolant temp did go up by 5 deg F. Some believe that external diffusion
may account for the increased effectiveness – but, I can’t see why
the external diffusion argument does not apply in all cases where the opening
is less than 1/3 the exit area. But, in any case, whatever the reason, I
am pleased with my cooling system.The left duct aircraft.jpb photo shows
the reduction in opening size with the new ducts. Those are the ones I am
currently flying with.
FWIW
Ed Anderson
Rv-6A N494BW Rotary Powered
Matthews, NC
eanderson@carolina.rr.com
http://www.andersonee.com
http://members.cox.net/rogersda/rotary/configs.htm#N494BW
http://www.dmack.net/mazda/index.html
From: Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of sboese
Sent: Thursday, October 23, 2008
6:02 PM
To: Rotary
motors in aircraft
Subject: [FlyRotary] staging
glitch and airspeeds
The flood gates are open again….
In response to Tracy’s question about trying the B
controller, It was my experience that the B controller always worked better
than the A. By programming the B controller directly, the staging glitch
could be essentially eliminated. After programming the A controller as
best as I could and copying those parameters to B, the glitch would appear in
the B controller but not nearly as pronounced as when the same parameters were
used with the A controller. I could never get the glitch to persist with
the B controller. I think this makes sense considering the information
provided by Tracy and Ed. Enriching the mixture upon staging may have
minimized the problem that was happening with the A controller, but mixture may
still have been too rich during staging when used with the stable B controller.
I have attached an image of the data
logged during a prolonged staging glitch. Also included is an image of
the staging region of the mixture map used by my modified system where no
staging glitch occurs. The map is unique to my system, of course, since
many variables are involved in developing a good mixture map. My system
may be simpler than some in that all four injectors are the same part number
and well matched. From previous investigations, I know the limits of the
linear range of the injector fuel delivery vs pulse width and I have increased
the MAP where staging occurs so the injectors are operating within this linear
range. With my setup, it has been possible to compensate for operating
the injectors at shorter pulse widths than the linear range to some extent by
programming the mixture table, but this seems to be operating on the ragged edge
of injector reliability and the effectiveness of this compensation seems
variable from day to day. In my opinion, there have been no problems
associated with having the injector staging point at MAP values closer to where
long term operation of the engine occurs. I’ve collected data where
the controller was changing rapidly between unstaged and staged operation and
the only way of knowing this was to examine the data after the fact. The
engine ran smoothly the whole time.
Based on the data collected and shown in
the attached image, I’m not even sure that the glitch has anything to do
with staging or even the mixture delivered to the engine. My fuel flow
indicator integrates the primary injector pulse time and doubles that when the
secondaries are being used. With 4 well matched injectors all operating
in the linear region, the fuel flow indication should be reliable. There
is no fuel flow anomaly seen in the data. The only deviations from
expected behavior are the lack of rpm increase with MAP and the O2 sensors
going lean (which are an indication of what is coming out of the engine- not
what’s going in). Is the whole fuel delivery system capable of
following an unstable MAP indication so quickly that individual injector pulses
are so lean or rich from one chamber to the next that misfiring occurs but the
average fuel delivery rate is still correct? The bottom line is
that the main flaw remaining in my system is my curiosity. Why should I
care what the problem was as long as it’s gone and stays away?
I’m working on that.
In response to Tracy’s comments on cooling drag and
airspeeds:
During the last month, I changed part of
the fuel system and eliminated the fuel transfer system with its associated
switches, timer and electric fuel pump. That was replaced by a duplex
fuel valve that I made (I couldn’t handle the price of Andair’s
duplex valve). Now I can just operate the valve and take fuel from either
tank and return it to the same tank with no electrical requirement. The
change in operational procedure is minimal: change the valve position
periodically instead of pushing a button, but decreased parts count and failure
modes are an improvement, I hope. Ed’s recent experience reinforces
my inclination toward two independent fuel sources. At least it’s
no longer possible to transfer fuel out the right tank’s vent, not that
I’ve ever done that, of course.
I exercised the fuel valve in the shop
(the screen, pumps and filters all easily come out of the plane by taking out 4
bolts and disconnecting the fuel lines and electrical wires) and verified its
operation even under conditions that should never happen in the plane.
The system passed all the tests I could think of. After reinstalling the
fuel module, I tied the plane down and made a ground run for 40 minutes at low
cruise power settings (7gal/hr fuel flow), changing the valve position every 5
minutes. Again everything worked fine.
The ground run was also a test of
alternator out flight endurance. With the alternators off, the battery
voltage was 10 volts after 40 minutes and the engine was still running
fine. This was with only the engine essential electrical systems powered
up. I should have made that test a long time ago instead of worrying
every time I flew, not knowing how long I could maintain altitude in the event
of alternator failure. The recent discovery of Steve Fossett’s
final destination, and realizing that on our return trip from CA we flew within
a few miles of that place if not directly over it, finally prompted me do this
endurance test. I’m quite sure that the time, effort, and expense
of the search for Steve Fossett would not have been expended looking for Steve
Boese.
What does this have to do cooling drag and
with airspeed? I’ve really never had problems from
insufficient cooling. If I can operate my plane tied down on the ground
for 40 minutes with an OAT of close to 70 deg F while burning 7 gal/hr of fuel
and not overheat, it seems quite possible that the cooling system still may not
be optimized. I’ve always had a thermostat installed in the water
pump housing which prevents the coolant temperatures from going too low.
In flight at higher power settings and
moderate temperatures, the thermostat is fully open, however, so I am not sure
the airflow through the cowling is excessive. The inlets to the coolant
radiators are unmodified from the original cowling configuration as supplied by
Van’s. My instrumentation shows that I am recovering over 90% of
pitot tube pressure at the coolant heat exchanger faces. The inlet to the
oil cooler is the same area as one of the original Van’s inlets and the
new duct to the oil cooler is long enough and shaped such that it seems likely
that internal pressure recovery is occurring in it. The coolant radiators
are so close to the air inlets that the duct shapes are definitely not
desirable and internal pressure recovery in them is unlikely. Since I
have good pressure recovery, this must be happening in front of the inlet
opening. Is this what is meant by external diffusion? Is a bubble
of high pressure air sitting at the front of the cowling while in flight?
If so, then the sensation of coming up against a wall while accelerating in
flight is more accurate than I thought. The wall is just transparent.
The change in the cowling shape and
reduction of the outlet area resulted in maybe over 5 knots increase in IAS but
not more than 10. That increase might be substantial at higher airspeeds,
but where I am stuck- probably not. Also, the fact that I can remove the
huge “bomb” and only gain 3 knots at most seems to indicate a high
degree of drag elsewhere and not just in the region of the cooling air
outlet. Other than having an oil cooler inlet slightly larger than the
original Van’s snorkel, the increased outlet area, and the
‘bomb”, the external configuration of my plane is standard
RV-6A and I have been told that my construction is as good as many
others. The concept of reaching a critical point in drag reduction is a
new one to me. In that context, my efforts and lack of positive results
start to make some sense.
Tracy, your analysis is more than likely correct (as usual) and I
am thankful for your input.
Steve
-----Original Message-----
From: Rotary
motors in aircraft [mailto:flyrotary@lancaironline.net] On Behalf Of Tracy Crook
Sent: Thursday, October 23, 2008
10:00 AM
To: Rotary
motors in aircraft
Subject: [FlyRotary] Re: N613BX
update
Here are some more comments about the MAP sensors for those
who are comfortable checking their own electronics hardware.
Steve's advice about output filters on MAP
sensors is good. I had noticed some instability on some (but not
all) Motorola pressure sensors so I have added a small capacitor (.1
uF) to their outputs on later versions of the EC2 and on the
EC3. I also add these on all updates if the unit does not already have
them. There is also another factor that affects this.
The first two versions of the EC2 board were layed out by an outside source.
The ground path for the map sensor was so long and convoluted that it
aggravated the tendency for instability on the sensor, especially on
controller A. This was also the cause of mixture going crazy on
controller A when transmitting on the radio in some installations.
Adding a short ground jumper from A controller MAP sensor ground to
the ground plane on the board fixed this problem. This jumper is also
added whenever I do updates. I was wondering if Steve had ever
tried switching to B and seeing if it had the same staging glitch. If the
problem was on A only, it may have been due to the ground problem.
Let me know if you tried that Steve. I'd recommend adding
the jumper in any case.
This same type of ground layout problem
caused the radio receiver noise (a hiss heard in the aircraft radio) on
the single part EM2. All affected EM2 customers were
notified to have them updated and I think all of them have been at this
point. This was the reason I quite having my PCB board layouts done by outside
sources. Just what I needed, another job :>)
Very surprised by your airspeed numbers
Steve. They are significantly lower than I would
expect. Your plane looks pretty clean except for the cooling
outlet. Purely speculation but I'm guessing that cooling drag is still
slowing you down. Both my -4 and -8 have only 50 sq in of cooling outlet
which means even after you reduced it by half you still have about
60% more outlet area than I do. Cooling problems can sometimes be
helped by enlarging the outlet but this is always a high drag
solution. I can't remember what kind of inlet ducting you have but
that is always the area where cooling improvements and drag reduction have been
found on my plane. BTW, did you notice much change in top or cruise
speed before vs after the outlet change? Until you get to the
critical point in reduction there is usually very little change.
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