Great and interesting report, Steve.
Thanks.
I had not thought about how different it
might seem to operate near the ground at a much lower density altitude –
aircraft performance on take off probably felt considerably stronger than at
7000 MLS {:>).
My best performance with the 2.17:1 and
68x72 prop was 196 MPH TAS at 5500 MSL (did not have my fuel flow meter at the
time).
My best performance with the current 2.85
and 74x88 prop was 200 MPH TAS 12.3 GPH burn rate at 9500 MSL. Pulling
back to 10.3 GPH gave 190 MPH TAS. But, I normally cruise at 7.5-8.5 GPH at
140-150 IAS – just too cheap to go anywhere in a big hurry {:>).
Interesting finding on your EC2 and the
manifold pressure sensors. If Motorola indicated a filter was good thing
to do, they undoubtedly had results indicating so. I noticed that at the
staging point my air/fuel indicator would run very quickly from rich to off the
scale lean. I could never figure out why it would do that. I
thought it might have to do with no fuel in the secondary runners before
staging and it taking a few milliseconds to get the fuel mixture down to the
combustion chamber – but the “glitch” was much longer than
that would account for and my secondaries are about as close as you can get
them to the ports. I ended up enriching the mixture (considerably) around
the staging point and that “solved” the problem for me. Well,
it really didn’t solve the problem since I could not figure out what it
was – but it makes the response acceptable.
Sounds like many folks encounter that
problem and you just may have found cause of the problem and a fix for
it. Thanks for the report on it. I agree with your recommendation
for folks not to go attempting to modify their EC2 – even if you are
successful in installing the filter components, there is always the possibility
of unintended consequences occurring else where in the system as a
results. Always a risk involved.
Thanks again for the very interesting
report.
From: Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of sboese
Sent: Wednesday, October 22, 2008
7:18 PM
To: Rotary
motors in aircraft
Subject: [FlyRotary] N613BX update
To anyone interested:
The following is a response to
Doug’s recent request for updates on flying rotaries:
In early June, having recovered sufficient
courage to try another cross country trip after feeding my prop to my tow bar (yes
Ed, I still have the tow bar) in Minnesota, we finally set out on another one
in our 13B powered RV-6A, this time to the west. After squeezing between
the top of the controlled airspace and a cloud layer over Great Salt Lake,
negotiating a narrow corridor which happened to be populated with
scattered rain showers between restricted airspaces, and a fuel stop in Wendover, UT, we crossed Mono Lake,
the Sierra Mountains,
and Yosemite Park at 14500 ft with 50 knot
headwinds. Thumbing my nose at the concept of shock cooling, we descended
over 11,000 ft in 25 miles and landed at our destination of Mariposa-Yosemite
airport. Other than a little initial roughness on bringing the power back
up in the pattern after that descent, probably due to some lead fowling of the
plugs since 100 LL was the only suitable fuel available at Wendover, the engine
installation behaved flawlessly. This is in contrast to the performance
of the pilot with the different sight picture at the slower ground speeds at
lower density altitude than I ever see at home in Laramie, WY, and the inclined
runway surrounded by hills at MPI. Thankfully, those details are not
rotary related however, and need not be expanded upon further.
The friends we stayed with near Mariposa
built an award-winning RV-6 with an O-360 and CS prop. While we were
there, we took a couple of side trips with the planes which gave the
opportunity for some side by side comparisons. Their take off and climb
performance was much more impressive than ours which was not surprising since
our Performance Propellers fixed pitch prop is set up primarily for cruise
rather than climb. On one trip, after flying a mile out over the Pacific
at Monterrey Bay (just to say we did it) I set
up the plane at max power and made the flight back to MPI under these
conditions. Altitude was 5500 ft, fuel burn was 14.8-15 gal/hr, MAP was
23.8”, RPM was 5900, and IAS was 148 knots. I don’t know what
the OAT was, but it wasn’t out of the ordinary. Our friends
reported burning close to 9 gal/hr while flying alongside us during this
time. I was somewhat surprised by this and one thing in particular came
to mind: parasite drag. The attached picture was taken during this flight
and two sources of drag can be readily seen: the large and sharp angled cooling
air outlet, and the “bomb” which is a muffler.
The trip home was relatively uneventful
and involved a detour over Mammoth
Lakes, CA to allow
more time to climb and a lower altitude for crossing the Sierras. At the
fuel stop at Wendover, I discovered a crack in one of the braces between the
rear of the engine and the exhaust header, but this wasn’t a particular
cause for worry since I had flown for more than 40 hrs before even installing
the two of those. Since we did not have headwinds on the return trip, the
total flight time home was an hour less than the flight time out. The
landing in Laramie
was in conditions not uncommon to this area, landing on runway 21 with the ASOS
reporting winds from 250 degrees at 22 gusting to 30. Thankfully, I had
completed a flight review using our plane just a few days before starting the
trip and crosswind technique was one of the things developed. At least
this was the last stop because the seat was definitely at risk of being soiled.
After returning home, a drag reduction
attempt was made by cutting away much of the bottom of the lower cowling and
reshaping the cooling air outlet to be much more similar to the original shape
as supplied by Van’s. This cut the outlet area approximately in
half to 77 sq in which is still larger than that in the unmodified original
cowling. This configuration is shown in another attached photo.
Tuft testing showed no turbulent areas except for one tuft right behind the
exhaust header outlet. Test flights at max power were conducted with and
without the “bomb”.
Without the
muffler: 163 knot TAS at 11500 ft DA, 12.4 gal/hr fuel flow, 5800 rpm,
19.9” MAP
With the muffler: 160 knot TAS at 11500 ft DA, 12.2 gal/hr
fuel flow, 5750 rpm. 20.2” MAP
The 3 knot penalty is a small price to pay
since the noise level without the muffler is unbearable for any length of time.
Cooling is still satisfactory but under
cowl temperatures are higher (~160 deg F) than before as would be expected with
decreased cooling air mass flow. An enclosure was constructed around the
stock Mazda ignition coils and a blast tube installed from the oil cooler air
inlet to this enclosure which keeps the coils at less than 110 deg F.
Several other changes have been made since
first flight over two years ago:
One is the elimination of the cowling
combustion air inlet (snorkel) and filtered air box as originally supplied by
Van’s. A NACA duct inlet and air filter was installed in the
cowling side very near the throttle body. This eliminated the over 3 foot
long 3.25 inch diameter skeet duct from the air box to the throttle body.
This was done to avoid the heating of the air while inside this duct which
resulted in temperatures of the air entering the throttle body in excess of 110
degrees F in flight regardless of the OAT. Now, the air entering the
throttle body remains within 2 degrees F of the OAT. The result is a
lower Density altitude seen by the engine.
Another change was the elimination of the
vacuum system which included the DG, AI, Mazda smog pump used as the vacuum
pump, vacuum regulator, and associated tubes and filters. In place of the
smog pump, a second alternator was installed. The second alternator led
me to eliminate the second PC680 battery. The instrumentation was
replaced by a Dynon D10A EFIS. A net weight decrease of 19 lb was
realized by these changes.
One other change that I made before the CA
trip involved problems I had with tuning the system to transition the injector
staging point without hesitation or misfiring of the engine. This had
always been of only slight concern until during one flight when advancing the
throttle after a stall, the engine hung up and didn’t produce full power
for almost 10 seconds. As best as I can remember since some sense of
panic ensued, first backing off the throttle position significantly from full
did not clear the condition, but tweaking the mixture control did.
The behavior seemed somewhat similar to SAG as described by others
on this list, but I could not correlate the event to spark plug
condition. Further attempts at tuning the mixture table in the staging
region were unsuccessful at eliminating this behavior. As also described
as having been tried by others on this list, I tried to pneumatically filter
the manifold pressure input to the EC2 using fuel filters and various sized
orifices in the lines between the plenum and EC2. It was possible to
induce surging with orifices of too small opening, but the staging difficulty
was not improved with various combinations of reservoir and orifice size.
During these tests, I found that by proper (improper?) manipulation of the
throttle, I could repeatedly induce the extended lack of power increase on
injector staging. Data recorded by my monitoring system clearly showed
the rpm plateau persisting while changing manifold pressure with the throttle,
average fuel flow consistent with the associated MAP at any given
instant, and a lean condition as shown by both O2 sensors. Since
the fuel flow was reasonable, the excess O2 could result from ineffective
ignition: fuel was there, but not being burned and using up the O2.
No faults with the ignition system could be found by tests including among
others checking the ignition timing and using new spark plugs and wires.
Since the condition could be induced by changing manifold pressure, I
postulated that the manifold pressure as seen by the EC2 may be unstable or
unreliable. Searching the Motorola literature on the sensors used in the
EC2, I found a reference to additional components recommended to be installed
on the sensor output if the output is connected to an A/D converter. In
desperation, I installed these components into my EC2 and immediately the
misbehavior on staging disappeared. I have not been able to induce it
again no matter how hard I try. My theory is that under certain
conditions, the MAP sensor output goes into oscillation which may or may not
persist depending on the circumstances. I have not verified this by
bringing the output signals external to the EC2 to an oscilloscope since if
they are subject to instability, doing so may provide more questions than
answers. I have pretty much kept this under my hat to this point, but
enough time on this change has been accumulated that I am comfortable that the
change is not detrimental at least. I certainly do NOT recommend or
encourage changes to the EC2 without Tracy’s
input without fully accepting the risks. I have no proof that my
interpretation of the events related above is correct, simply that it helped in
my individual case.
I had hoped to make it to the roundup this
year, having bought the charts, planned the flight and arranging time
off. The front that Bill managed to cross was too much to try to take on
from this far away. So here I sit watching the blowing snow outside
wishing that I had made it to the roundup and that the front had materialized
after getting there and thus preventing my return.
One additional note for those who made it
this far. I’ve been spending considerable time in our local ice
cream parlor in an attempt to maintain a constant system in-flight gross weight
after the elimination of the hardware as described above.
OOOOH the sacrifices one has to make in
the name of research….
Steve Boese
RV-6A, 1986 13B NA, EC2, RD1A …
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