Return-Path: Sender: (Marvin Kaye) To: lml Date: Sun, 12 May 2002 10:43:36 -0400 Message-ID: X-Original-Return-Path: Received: from smtp.comcast.net ([24.153.64.2] verified) by logan.com (CommuniGate Pro SMTP 4.0b1) with ESMTP id 1235478 for lml@lancaironline.net; Sun, 12 May 2002 10:00:40 -0400 Received: from cc1860069a (pcp01159375pcs.rocsth01.mi.comcast.net [68.62.25.175]) by mtaout04.icomcast.net (iPlanet Messaging Server 5.1 HotFix 0.6 (built Apr 26 2002)) with SMTP id <0GW000B05495AA@mtaout04.icomcast.net> for lml@lancaironline.net; Sun, 12 May 2002 10:00:41 -0400 (EDT) X-Original-Date: Sun, 12 May 2002 10:00:56 -0400 From: edechazal@comcast.net Subject: LNC2 Hydraulics X-Original-To: Lancair Mailing List X-Original-Message-id: <00a501c1f9bd$702e4420$af193e44@rocsth01.mi.comcast.net> MIME-version: 1.0 X-MIMEOLE: Produced By Microsoft MimeOLE V5.50.4133.2400 X-Mailer: Microsoft Outlook Express 5.50.4133.2400 Content-type: text/plain; charset=iso-8859-1 Content-transfer-encoding: 7BIT X-Priority: 3 X-MSMail-priority: Normal References: I just finished a messy and protracted job of hunting down and fixing an internal hydraulic leak on my 360. The system would hold pressure for only a few minutes on the ground before the pump would cycle. In the air it was about a half hour. Having reached this far down the squawk list of annoyances, I decided it was time to put the plane on jacks and finally fix this. I have hydraulic pressure gages on the panel so I decided to progressively remove components until the pressure stabilized. I would fix the offending component and declare victory. Not so simple. As I removed parts and capped off the lines, I could see improvement but not complete satisfaction. Finally, I had nothing but the pump and the gages in the circuit and decided that pressure was holding so I declared the pump OK. Next I decided to go ahead and rebuild the nose gear cylinder and it's door cylinder since I judged these suspects from the preceding tests. The nose gear cylinder required a call to the Aero-Tek factory to figure out how to get it apart. Hint: remove the 90 degree elbow fittings first. When I inspected the cylinder inside wall I discovered significant scoring and metal grit around the O-rings. I had found my smoking gun. The scoring was worse where the piston sits in gear down. Makes sense as this is where particles might collect. I got new cylinder tubes from Aero-tek for about one third of the cost of new assemblies and reassembled everything. I decided that the main gear cylinders should receive identical treatment and these proved to be scored too but less so. I also removed the pump and cleaned out the reservoir. There was a lot of black soot at the bottom which I'm certain was telltale of my problems. Hydraulic pressure (about half) now remains even over night which is plenty. This system finally behaves itself. The moral of this story is that I needed to be far more sanitary during construction to keep the grit out of the system. The Aero-Tek engineer said the fiberglass grit really eats them up. And don't reuse fluid. I tried to economize by running used fluid back through a paper towel filter. This is just dumb and not worth the small savings since the black soot doesn't get filtered out. Ed de Chazal N361DC