|
I am keeping you in mind, Thomas. I have
been building for seems like forever and I am not really anxious to take the
plane down and start on another install right now. I am still flying off my
Phase 1!
Bill
From: Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of Thomas Giddings
Sent: Tuesday, May 15, 2012 6:03
PM
To: Rotary
motors in aircraft
Subject: [FlyRotary] Re: Fuel Flow
Bill: I still have that 20B here in Ft Myers. complete with intake
,throttle bodies and Rotrex Super Charger if you need more power:)
On May 15, 2012, at 5:55 PM, Bill Bradburry wrote:
I know. I discussed with them making
a 20B plate with ears for the 13B on it. They could have even put ears
for both the 20 and the 13B by just not hogging off the entire side. If
you look at how the plate is designed, it will be clear to you what I
mean. Anyway, they didn’t seem interested in the project. I have no
idea why but it would have worked perfectly for my install. If I
decide to go with the 20B, I suppose I will just have to have the plate made
somewhere locally. I didn’t want to have to do my own figuring about
where all the oil pan bolts go, but….??!!
Bill
From: Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of argoldman@aol.com
Sent: Tuesday, May 15, 2012 1:13
PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Re: Fuel Flow
Bill,
I don't know if you are aware but the Girllllllllls do make a plate for the 20,
as well as an engine mount. Look at their site
-----Original
Message-----
From: Bill Bradburry <bbradburry@bellsouth.net>
To: Rotary motors in
aircraft <flyrotary@lancaironline.net>
Sent: Tue, May 15, 2012 10:34 am
Subject: [FlyRotary] Re: Fuel Flow
The Renesis has a 10:1 compression
ratio. Are you sure you are not getting detonation at high (30-40)
manifold pressures and low (1700 prop) rpms? These considerations and the
fact that I just don’t have room to squeeze it in are the reasons that I
decided against a turbo. The stock (car) engine has a knock sensor, but
we don’t have any way to monitor it and with the noise and headsets to cancel
it out, I doubt that we would ever hear detonation unless engine parts were
flying past our ears. :>)
I would like a little more power, but for
me, it would be easier to install a 20B than to switch to a turbo. I have
enough room behind the engine that a 20B would set on my existing motor
mount. All I would have to do is make up a mount plate for the 20B that
has the mounting ears in the positions of the 13B ears. I could even use
a little more weight in the front for W&B, so the extra weight would also
probably work well also. My plane is heavier than a RV6/7 by about 500 lbs, so
I could use the HP on takeoff and same for cruise as well.
I briefly touched on this mount plate idea
a year or so ago with the Cozy Girrls, but they didn’t seem to be interested in
making the mount plate although it would be pretty simple to leave 13B as well
as 20B ears on a 20B mount.
The rotary HP is really a factor of the
rpm. When you dial it down in rpm, the HP drops to that level. I am
not certain what effect the turbo would have on this number, but for NA engine,
5K rpm is about 160 HP, 6K=180, 7K=200, etc.
This is pretty close to the same on all
the Dyno graphs that I have seen. Pretty much no matter how “souped up”
the engine is, it still follows that same HP curve. This becomes a
problem for those of us who want to develop 200HP but run at 5K rpm. That
aint gonna happen with the two rotor engine. :>(
From: Rotary motors in aircraft [mailto:flyrotary@lancaironline.net]
On Behalf Of Bobby J. Hughes
Sent: Tuesday, May 15, 2012 10:02
AM
To: Rotary motors in aircraft
Subject: [FlyRotary] Fuel Flow
This configuration is
my sweet spot. Efficiency declines rapidly with faster rpm. I can also
run the same prop rpm at a lower manifold pressure 24-26 “and see almost the
same fuel burn at 150 mph TAS. Increasing the manifold pressure to 30 or a
little higher increases speed but the fuel burn barely increases. At the other
extreme with prop set to 2350-2400, 30 -32” MP I see a top speed of 190 mph but
the fuel burn shows 16 gph. Not good. The lyc RV10’s are way more efficient at
this speed. I suspect the super charger drive losses are a big factor at the
high power settings. Possibly up to 2 gph? It’s possible the
fuel flow is not accurate in the high power configuration. I’m not
comfortable running the engine that hard for very long so calibration verification
is not possible. I’ve been reconsidering a turbo but still not convinced
the renesis exhaust ports are up to the abuse. Although a looser turbo may
eliminate the housing damage that has occurred in the turbo RX8’s.
I wonder what intercooled, 38” MP at 1900 rpm would do for speed and fuel burn?
From: Rotary motors in aircraft [mailto:flyrotary@lancaironline.net]
On Behalf Of Charlie England
Sent: Monday, May 14, 2012 8:57 PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Re: Thanks Tracy!
Hi Bobby,
Those are pretty good numbers for a 4seat plane, even a -10, at that fuel flow.
Have you checked it at around 11gph?
Thanks,
Charlie
On 05/14/2012 03:26 PM, Bobby J. Hughes wrote:
Cruise rpm is
typically 1700-1825 prop \ 4850-5200 engine. The low rpm may influence my
EGT’s. In this configuration I see 160-165 MPH TAS at 8-8.5 gph at 6000 foot.
It does a little better up high.
I see around 1650F
max. At cruise altitude running less than 30”MP I can lean to about 1475F.
From: Rotary
motors in aircraft [mailto:flyrotary@lancaironline.net] On Behalf Of Bill
Bradburry
Sent: Saturday, May 12, 2012 7:06
PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Thanks Tracy!
The EM-2 mixture is working fine now, Tracy.
I appreciate the rapid turnaround.
I wanted to ask you about the EGTs I
should expect from the Renesis. I am getting EGTs in the upper 17s.
I think I expected them to be a couple of hundred lower than that. I
don’t doubt the accuracy because the EGTs report a pretty accurate OAT when I
first arrive at the hangar and before I start the engine.
I did some relearning of the EC-2 during
the flight today between 18 and 29 inches manifold pressure. This was
done at 2K feet. The MAP was lowered considerably and now the mid point
of the graph is pretty close to the knob center, maybe 12:30-1:00 o’clock.
A good explanation of how to lean would be
very helpful for me at this point. Also I am wondering what fuel burn
most are getting at cruise. I am still calibrating this function, but I
would like to know what to expect if I ever get it right.
|
|