X-Virus-Scanned: clean according to Sophos on Logan.com Return-Path: Received: from mail-fx0-f52.google.com ([209.85.161.52] verified) by logan.com (CommuniGate Pro SMTP 5.4.1) with ESMTPS id 5085689 for flyrotary@lancaironline.net; Mon, 08 Aug 2011 13:22:14 -0400 Received-SPF: pass receiver=logan.com; client-ip=209.85.161.52; envelope-from=wdleonard@gmail.com Received: by fxd18 with SMTP id 18so2259702fxd.25 for ; Mon, 08 Aug 2011 10:21:38 -0700 (PDT) DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=gmail.com; s=gamma; h=mime-version:in-reply-to:references:date:message-id:subject:from:to :content-type; bh=MtR83p6IqljPiz/u/SqPW19cCihYOYlQQ7gJzF1hjBs=; b=ledhhWD+NQpr72GewHKI89W8UbJbuzrXiGPgKpHcV+HXKTLJ6kjYRJBvThBwmzt2Wu rj+qHmchLSpTphmwLl9s9yJSe0bLk9vmL41cPJvPDsYl/QdPOaprIGO7NUawbpE9toNK Xn4lv/QRX8cjrVQiLhwLv5l1NkErW4g1TSabE= MIME-Version: 1.0 Received: by 10.223.134.88 with SMTP id i24mr7796609fat.68.1312824097539; Mon, 08 Aug 2011 10:21:37 -0700 (PDT) Received: by 10.223.69.132 with HTTP; Mon, 8 Aug 2011 10:21:37 -0700 (PDT) In-Reply-To: References: Date: Mon, 8 Aug 2011 10:21:37 -0700 Message-ID: Subject: Re: [FlyRotary] Sam Hodge Force landing - All OK From: David Leonard To: Rotary motors in aircraft Content-Type: multipart/alternative; boundary=00235453067cfc883604aa01adb8 --00235453067cfc883604aa01adb8 Content-Type: text/plain; charset=ISO-8859-1 Really glad to hear that Sam and his wife are OK. Very nicely done. Always sad to hear about damaged aircraft. But... NEVER take a passenger on a shake-down flight. Curious to hear the cause, and also the the changes that were made just before the flight. -- David Leonard Turbo Rotary RV-6 N4VY http://N4VY.RotaryRoster.net http://RotaryRoster.net On Mon, Aug 8, 2011 at 9:12 AM, Ed Anderson wrote: > ** > Sam Hodges just called me to tell me about his forced landing after take > off at Paducha on 7 August. Ed K had notified me the day before of the > incident but I wanted to get more details from Sam before reporting. > > Engine sputtered and quit approx 200-300 ft after take off - Sam stated he > had time to switch from A to B controller - but it made no difference. It > was a hot 97F day. Sam had performed runup before take off and all appeared > OK. > > Sam made it to a dirt road after the engine quit, but the nose gear failed > and the aircraft also incurred some damage to the wing tips. He and his > spouse Rose were shaken up a bit but bascially OK except for sore muscles, > etc. > > Sam is meeting FAA guy to go over the aircraft - back at the hangar- > today. > > As those of you who make it to the Paducha flyin last fall know - Sam and > Rose have a beautifuly Renesis installation in an RV-7A - a really nice > looking package. > > Sam has been working out the bugs of his installation - wrestling with > temperatures primarily and this flight was to check out the effectiveness of > some of his recent changes. > > I'm sure Sam will let us know whatever is uncovered pertinent to the > incident. > > Just great that no one was seriously injured or worst > > Ed > > Edward L. Anderson > Anderson Electronic Enterprises LLC > 305 Reefton Road > Weddington, NC 28104 > http://www.andersonee.com > http://www.eicommander.com > --00235453067cfc883604aa01adb8 Content-Type: text/html; charset=ISO-8859-1 Content-Transfer-Encoding: quoted-printable Really glad to hear that Sam and his wife are OK. =A0Very nicely done. =A0A= lways sad to hear about=A0damaged=A0aircraft.

But... =A0= NEVER take a passenger on a shake-down flight.

Cur= ious to hear the cause, and also the the changes that were made just before= the flight.

--=A0
David Leonard

Turbo Rotary RV-6 N4VYhttp://N4VY.RotaryRoster.net<= br>http://RotaryRoster.net

<= div class=3D"gmail_quote"> On Mon, Aug 8, 2011 at 9:12 AM, Ed Anderson <eanderson@carolina.rr.com> wrote:
Sam Hodges just called me to tell me about his fo= rced=20 landing after take off at Paducha on 7 August.=A0 Ed K had notified me the= =20 day before of the incident but I wanted to get more details from Sam before= =20 reporting.
=A0
Engine sputtered and quit approx 200-300 ft after= take off=20 -=A0 Sam stated he had time to switch from A to B controller - but it made = no=20 difference.=A0 It was a hot 97F day.=A0 Sam had performed runup before=20 take off and all appeared OK.
=A0
Sam made it to a dirt road after the engine quit,= but the=20 nose gear failed and the aircraft also incurred some damage to the wing=20 tips.=A0 He and his spouse Rose were shaken up a bit but bascially OK excep= t=20 for sore muscles, etc.
=A0
Sam is meeting FAA guy to go over the aircraft - = back at=20 the hangar- today.=A0
=A0
As those of you who make it to the Paducha flyin = last fall=20 know - Sam and Rose have a beautifuly Renesis installation in an RV-7A - a= =20 really nice looking package.
=A0
Sam has been working out the bugs of his installa= tion -=20 wrestling with temperatures primarily and this flight was to check out the= =20 effectiveness of some of his recent changes.
=A0
I'm sure Sam will let us know whatever is unc= overed=20 pertinent to the incident.
=A0
Just great that no one was seriously injured or= =20 worst
=A0
Ed
=A0
Edward L. Anderson
Anderson Electronic Enterpr= ises=20 LLC
305 Reefton Road
Weddington, NC 28104
http://www.andersonee.com
http://www.eicommander.com




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