X-Virus-Scanned: clean according to Sophos on Logan.com Return-Path: Received: from mail-fx0-f52.google.com ([209.85.161.52] verified) by logan.com (CommuniGate Pro SMTP 5.4.1) with ESMTPS id 5085638 for flyrotary@lancaironline.net; Mon, 08 Aug 2011 12:31:25 -0400 Received-SPF: pass receiver=logan.com; client-ip=209.85.161.52; envelope-from=msteitle@gmail.com Received: by fxd18 with SMTP id 18so2215255fxd.25 for ; Mon, 08 Aug 2011 09:30:47 -0700 (PDT) DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=gmail.com; s=gamma; h=mime-version:in-reply-to:references:date:message-id:subject:from:to :content-type; bh=CVdPycvgrfyibvidFyHY0NCnSDFSKDJ1TlQrq0Arx1I=; b=KSnDTOlB/0qxmp0Jd6vwSznBgeU0zZKyu/gP4hwADTiDVv5HRtmSHylp3foAMlD8xG RLd4bOA1vMgirZG4fWWjUOBIbJMoMt5NpnPjXHoLBYsxHG3GtQvMwWQi9dj9wseRsdbE ADKH97BwFxzPCpfa1jpJWAmo31Iq+EAmuTcKU= MIME-Version: 1.0 Received: by 10.223.127.195 with SMTP id h3mr51480fas.135.1312821046831; Mon, 08 Aug 2011 09:30:46 -0700 (PDT) Received: by 10.223.83.194 with HTTP; Mon, 8 Aug 2011 09:30:46 -0700 (PDT) In-Reply-To: References: Date: Mon, 8 Aug 2011 11:30:46 -0500 Message-ID: Subject: Re: [FlyRotary] Sam Hodge Force landing - All OK From: Mark Steitle To: Rotary motors in aircraft Content-Type: multipart/alternative; boundary=00235407f006266a7004aa00f829 --00235407f006266a7004aa00f829 Content-Type: text/plain; charset=ISO-8859-1 Ed, Very happy to hear of Sam's successful engine-out landing. While there was damaged sheet metal, and frayed nurves, by landing straight ahead they were able to walk away. Good job Sam! Please let us know what you find as to the cause. It sure would be nice to have data-logging capabilities on the EC-2/EM-2. Mark On Mon, Aug 8, 2011 at 11:12 AM, Ed Anderson wrote: > ** > Sam Hodges just called me to tell me about his forced landing after take > off at Paducha on 7 August. Ed K had notified me the day before of the > incident but I wanted to get more details from Sam before reporting. > > Engine sputtered and quit approx 200-300 ft after take off - Sam stated he > had time to switch from A to B controller - but it made no difference. It > was a hot 97F day. Sam had performed runup before take off and all appeared > OK. > > Sam made it to a dirt road after the engine quit, but the nose gear failed > and the aircraft also incurred some damage to the wing tips. He and his > spouse Rose were shaken up a bit but bascially OK except for sore muscles, > etc. > > Sam is meeting FAA guy to go over the aircraft - back at the hangar- > today. > > As those of you who make it to the Paducha flyin last fall know - Sam and > Rose have a beautifuly Renesis installation in an RV-7A - a really nice > looking package. > > Sam has been working out the bugs of his installation - wrestling with > temperatures primarily and this flight was to check out the effectiveness of > some of his recent changes. > > I'm sure Sam will let us know whatever is uncovered pertinent to the > incident. > > Just great that no one was seriously injured or worst > > Ed > > Edward L. Anderson > Anderson Electronic Enterprises LLC > 305 Reefton Road > Weddington, NC 28104 > http://www.andersonee.com > http://www.eicommander.com > --00235407f006266a7004aa00f829 Content-Type: text/html; charset=ISO-8859-1 Content-Transfer-Encoding: quoted-printable
Ed,
=A0
Very happy to hear=A0of Sam's=A0successful engine-out landing.=A0 = While there was damaged sheet metal, and frayed nurves, by landing=A0straig= ht ahead they were able to walk away.=A0=A0Good job Sam!=A0 Please let us k= now what you find as to the cause.=A0 =A0
=A0
It sure would be nice to have data-logging capabilities on the EC-2/EM= -2.=A0
=A0
Mark

On Mon, Aug 8, 2011 at 11:12 AM, Ed Anderson <eanderson@c= arolina.rr.com> wrote:
Sam Hodges just called me to tell me about his fo= rced landing after take off at Paducha on 7 August.=A0 Ed K had notified me= the day before of the incident but I wanted to get more details from Sam b= efore reporting.
=A0
Engine sputtered and quit approx 200-300 ft after= take off -=A0 Sam stated he had time to switch from A to B controller - bu= t it made no difference.=A0 It was a hot 97F day.=A0 Sam had performed runu= p before take off and all appeared OK.
=A0
Sam made it to a dirt road after the engine quit,= but the nose gear failed and the aircraft also incurred some damage to the= wing tips.=A0 He and his spouse Rose were shaken up a bit but bascially OK= except for sore muscles, etc.
=A0
Sam is meeting FAA guy to go over the aircraft - = back at the hangar- today.=A0
=A0
As those of you who make it to the Paducha flyin = last fall know - Sam and Rose have a beautifuly Renesis installation in an = RV-7A - a really nice looking package.
=A0
Sam has been working out the bugs of his installa= tion - wrestling with temperatures primarily and this flight was to check o= ut the effectiveness of some of his recent changes.
=A0
I'm sure Sam will let us know whatever is unc= overed pertinent to the incident.
=A0
Just great that no one was seriously injured or w= orst
=A0
Ed
=A0
Edward L. Anderson
Anderson Electronic Enterpr= ises LLC
305 Reefton Road
Weddington, NC 28104
http://www.andersonee.com
http://www.eicommande= r.com

--00235407f006266a7004aa00f829--