Ed,
The Advanced EFIS
provides voice alerts for most engine parameters. I received no other alert but
AOA. However they
did not include egt’s with the water cooled package. It’s was designed for the
Egg subi’s and they would not modify for any other options. So if it was a
blockage would the egt’s have gone cold? Would a partial blockage raise the
egt’s?
Bobby
From:
Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of Ed Anderson
Sent: Sunday, March 20, 2011 6:21
PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Re: Forced Landing.
Altitude has been the saver in both
of my engine out events - I always go cross country at 8000MSL +
{:>)
Keeping your head cool and paying
attention to what your instruments are telling you (nice AOA system) is clearly
crucial.
Sent: Sunday,
March 20, 2011 9:19 PM
Subject:
[FlyRotary] Re: Forced Landing.
Thanks Ed. It happened
at the perfect airport with three long runways. I had executed a Vx climbing
turn at 38” MP. I had a lot of altitude and was very aware of the runway off my
right wing tip. Had this happened 5 minutes later it would be a completely
different story. Bobby
From:
Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of Ed Anderson
Sent: Sunday, March 20, 2011 6:01
PM
To: Rotary motors in aircraft
Subject: [FlyRotary] Re: Forced Landing.
Ain't it amazing how long 10 seconds
can seem when your heart is pounding and your mind racing - been
there!
As many an old instructor has
emphasized - first priority is FLY THE AIRCRAFT which you clearly did an
excellent job of.
I fly with two HushpowerII mufflers
(several hundred hours on them), but I have two headers each with their own
muffler. I fly with a turbo block which means no exhaust splitters to
soften the exhaust pulse - and it can rapidly pound stainless steel (or anything
else) into pieces. While I have never had exhaust blockage, I have
had internal pieces depart the muffler. I suspect after
several hundred hours my Hushpower II mufflers no longer have much of
anything internal but the metal mesh cone
remaining.
While a turbocharger would probably
soften the exhaust pulse quite a bit - a supercharger as you fly with, of
course, will not.
Well, it clear that there was little
you could do in the air about the muffler blockage - had I been a bit more
astute, I could have probable recovered engine power on my two unintentional
engine outs. Hindsight is just so wonderful
{:>)
Good flying, good decisions and it
ended well - well, except perhaps for your seat
cushion.
Sent: Sunday,
March 20, 2011 4:02 PM
Subject:
[FlyRotary] Forced Landing.
Since it’s been so quiet lately.
I had a complete loss of engine power yesterday during
climb out from Tyler TX (KTYR). I had executed a Vx climb to see you hot I could
get the oil with the supplemental oil cool I recently added. The engine was
running but stopped making any power. I switch fuel tanks, adjusted the mixture
both directions, toggled the primary injector switch for cold start and check my
breakers. I did everything but switch to the B controller. All the
troubleshooting took place in about 10 seconds or less. At that time my AOA
starting telling me “angle, angle, push, push” . Glad I had the AOA as I’m not
sure my attention was focused on the right priorities. I told the tower I had an
engine failure and was landing. 35. Very happy this happened at an airport with
three long runways with different headings. I pointed the nose down and made a
right turn to the runway. The landing was downwind with 15 knot wind. I was too
fast and used all 3500ft I had left. I coasted onto a taxiway with the engine
idling very rough. I couldn’t make enough power to taxi. The FBO was there
within two minutes and towed me back to their hanger. At this point I figured I
had lost an apex seals. I pulled the prop through but had good compression. I
pulled the cowl and everything was in place. Up until now I had remained very
calm but that changed when I realized there was no smoking gun. I checked my
injector power connections at the switches but everything seem good. The EC2
coil test worked but the injector test did not. I attempted an engine start and
it ran normally. “What the h***” I later realized I had not activated the cold
start switch for the injector test. Injectors tested fine. I was at a complete
loss as what to look at next. I thought about a CAS intermediate failure but
nothing I could come up with fit the problem. After another five minute full
power run to 38”MP on both controllers I rolled the plane back into the FBO’s
hanger and took a break. So here I am 200 miles from home after a forced landing
and the plane is making full power as usual. Now the nerves set in full force.
It downed on me to check the muffler for blockage. From what I could see with a
flashlight the cone in my HushpowerII was out of place. I dropped the muffler
from the belly and about a ½” cup of material came out. It was small pieces of
mess from the cone. About 1/3 of the entrance side cone was still intact but the
rest was gone. The internal steel support that forms the cone was still intact
but movable with a large screw driver. I knocked as much out as I could and
reinstalled the muffler. I was unable to knock out any of the mesh that was
still in place. I decided to conduct a flight test over the airport for ten
minutes. If all was good then I would head for home and climb to 8500 for the
trip back. The headwind at 8500 would add 20 minutes to the flight unless I ran
the engine above 30” MP. I didn’t think it was a good time to stress the muffler
any more than necessary. I took off and climbed to 3000 ft on the B controller
and circled for several laps. I switched controllers, fuel, injector cold start,
coils and everything was normal. So I nervously departed for the 200 mile trip.
I picked up flight following and had the autopilot/ flight director take me
home. I spent the entire flight with the nearest airport active on my Advanced
EFIS moving map. It draws a line, gives a distance and runway lengths. I also
check airport information on my ipad and Foreflight. The flight was uneventful
but was the most stressful I have ever experienced.
I’m guessing the muffler internals came loose and slid
rearward trapping all the small come material that was dislodged. I was
somewhere between Vx and Vy at a very high angle of attack when the problem
occurred. The muffler is parallel l with the bottom of the fuselage so I believe
any small dislodged material would remain inside the muffler. The plan now is to
go through the entire electrical system and check every connection associated
with the EC2 and fuel delivery. I will also be looking for a different muffle
and putting the plane back into flight testing until I can regain my confidence
with the install. I am also very thankful none of my family was onboard. My
teenage daughter had decided she didn’t want to spend the remainder of spring
break with me visiting my sister.
Bobby Hughes
(shaken not stirred)---- check your
mufflers!!!!
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