Bobby,
That is an excellent job of both flying
and troubleshooting to discover the cause of the problem. I am wondering why
you have a muffler if you have a turbo?
My Hushpower is welded in and up inside
the cowl. I would not be able to see inside if or remove or replace it with
the current setup. This incident has really made me start to think about the
muffler.. Thanks for the great report!
Bill B
From: Rotary motors in aircraft
[mailto:flyrotary@lancaironline.net] On
Behalf Of Bobby J. Hughes
Sent: Sunday, March 20, 2011 4:02
PM
To: Rotary
motors in aircraft
Subject: [FlyRotary] Forced
Landing.
Since it’s been so quiet lately.
I had a complete loss of engine power yesterday during climb out from
Tyler TX (KTYR). I had executed a Vx climb to see you hot I could get the oil with
the supplemental oil cool I recently added. The engine was running but stopped
making any power. I switch fuel tanks, adjusted the mixture both directions,
toggled the primary injector switch for cold start and check my breakers. I did
everything but switch to the B controller. All the troubleshooting took place
in about 10 seconds or less. At that time my AOA starting telling me
“angle, angle, push, push” . Glad I had the AOA as I’m not
sure my attention was focused on the right priorities. I told the tower I had
an engine failure and was landing. 35. Very happy this happened at an airport
with three long runways with different headings. I pointed the nose down and
made a right turn to the runway. The landing was downwind with 15 knot wind. I
was too fast and used all 3500ft I had left. I coasted onto a taxiway with the
engine idling very rough. I couldn’t make enough power to taxi. The FBO
was there within two minutes and towed me back to their hanger. At this point I
figured I had lost an apex seals. I pulled the prop through but had good
compression. I pulled the cowl and everything was in place. Up until now I had
remained very calm but that changed when I realized there was no smoking gun. I
checked my injector power connections at the switches but everything seem good.
The EC2 coil test worked but the injector test did not. I attempted an engine
start and it ran normally. “What the h***” I later realized I had
not activated the cold start switch for the injector test. Injectors tested fine.
I was at a complete loss as what to look at next. I thought about a CAS
intermediate failure but nothing I could come up with fit the problem. After
another five minute full power run to 38”MP on both controllers I rolled
the plane back into the FBO’s hanger and took a break. So here I am 200
miles from home after a forced landing and the plane is making full power as
usual. Now the nerves set in full force. It downed on me to check the muffler
for blockage. From what I could see with a flashlight the cone in my HushpowerII
was out of place. I dropped the muffler from the belly and about a ½” cup
of material came out. It was small pieces of mess from the cone. About 1/3 of
the entrance side cone was still intact but the rest was gone. The internal
steel support that forms the cone was still intact but movable with a large
screw driver. I knocked as much out as I could and reinstalled the muffler. I
was unable to knock out any of the mesh that was still in place. I decided to
conduct a flight test over the airport for ten minutes. If all was good then I
would head for home and climb to 8500 for the trip back. The headwind at 8500
would add 20 minutes to the flight unless I ran the engine above 30” MP.
I didn’t think it was a good time to stress the muffler any more than
necessary. I took off and climbed to 3000 ft on the B controller and circled
for several laps. I switched controllers, fuel, injector cold start, coils and
everything was normal. So I nervously departed for the 200 mile trip. I picked
up flight following and had the autopilot/ flight director take me home. I
spent the entire flight with the nearest airport active on my Advanced EFIS
moving map. It draws a line, gives a distance and runway lengths. I also check
airport information on my ipad and Foreflight. The flight was uneventful but
was the most stressful I have ever experienced.
I’m guessing the muffler internals came loose and slid rearward
trapping all the small come material that was dislodged. I was somewhere
between Vx and Vy at a very high angle of attack when the problem occurred. The
muffler is parallel l with the bottom of the fuselage so I believe any small
dislodged material would remain inside the muffler. The plan now is to go
through the entire electrical system and check every connection associated with
the EC2 and fuel delivery. I will also be looking for a different muffle and
putting the plane back into flight testing until I can regain my confidence
with the install. I am also very thankful none of my family was onboard. My
teenage daughter had decided she didn’t want to spend the remainder of
spring break with me visiting my sister.
Bobby Hughes
(shaken not stirred)---- check your mufflers!!!!