Since it’s been so quiet lately.
I had a complete loss of engine power yesterday during climb out from
Tyler TX (KTYR). I had executed a Vx climb to see you hot I could get the oil
with the supplemental oil cool I recently added. The engine was running but
stopped making any power. I switch fuel tanks, adjusted the mixture both
directions, toggled the primary injector switch for cold start and check my
breakers. I did everything but switch to the B controller. All the
troubleshooting took place in about 10 seconds or less. At that time my AOA
starting telling me “angle, angle, push, push” . Glad I had the AOA
as I’m not sure my attention was focused on the right priorities. I told
the tower I had an engine failure and was landing. 35. Very happy this happened
at an airport with three long runways with different headings. I pointed the
nose down and made a right turn to the runway. The landing was downwind with 15
knot wind. I was too fast and used all 3500ft I had left. I coasted onto a
taxiway with the engine idling very rough. I couldn’t make enough power
to taxi. The FBO was there within two minutes and towed me back to their
hanger. At this point I figured I had lost an apex seals. I pulled the prop
through but had good compression. I pulled the cowl and everything was in
place. Up until now I had remained very calm but that changed when I realized
there was no smoking gun. I checked my injector power connections at the
switches but everything seem good. The EC2 coil test worked but the injector
test did not. I attempted an engine start and it ran normally. “What the
h***” I later realized I had not activated the cold start switch for the
injector test. Injectors tested fine. I was at a complete loss as what to look
at next. I thought about a CAS intermediate failure but nothing I could come up
with fit the problem. After another five minute full power run to 38”MP
on both controllers I rolled the plane back into the FBO’s hanger and
took a break. So here I am 200 miles from home after a forced landing and the
plane is making full power as usual. Now the nerves set in full force. It
downed on me to check the muffler for blockage. From what I could see with a
flashlight the cone in my HushpowerII was out of place. I dropped the muffler
from the belly and about a ½” cup of material came out. It was small
pieces of mess from the cone. About 1/3 of the entrance side cone was still
intact but the rest was gone. The internal steel support that forms the cone
was still intact but movable with a large screw driver. I knocked as much out
as I could and reinstalled the muffler. I was unable to knock out any of the
mesh that was still in place. I decided to conduct a flight test over the
airport for ten minutes. If all was good then I would head for home and climb
to 8500 for the trip back. The headwind at 8500 would add 20 minutes to the
flight unless I ran the engine above 30” MP. I didn’t think it was
a good time to stress the muffler any more than necessary. I took off and
climbed to 3000 ft on the B controller and circled for several laps. I switched
controllers, fuel, injector cold start, coils and everything was normal. So I
nervously departed for the 200 mile trip. I picked up flight following and had
the autopilot/ flight director take me home. I spent the entire flight with the
nearest airport active on my Advanced EFIS moving map. It draws a line, gives a
distance and runway lengths. I also check airport information on my ipad and
Foreflight. The flight was uneventful but was the most stressful I have ever
experienced.
I’m guessing the muffler internals came loose and slid rearward
trapping all the small come material that was dislodged. I was somewhere between
Vx and Vy at a very high angle of attack when the problem occurred. The muffler
is parallel l with the bottom of the fuselage so I believe any small dislodged
material would remain inside the muffler. The plan now is to go through the
entire electrical system and check every connection associated with the EC2 and
fuel delivery. I will also be looking for a different muffle and putting the
plane back into flight testing until I can regain my confidence with the install.
I am also very thankful none of my family was onboard. My teenage daughter had
decided she didn’t want to spend the remainder of spring break with me
visiting my sister.
Bobby Hughes
(shaken not stirred)---- check your mufflers!!!!