The following observations may be of
interest in the light of recent discussions.
On the flight to the resent Rotorfest, I
thought the exhaust noise level had increased at one point. This was just chalked
up to fatigue and the longer than normal time in flight since this was the
longest XC attempted to date. My usual procedure for adjusting throttle
position is to advance it until no further increase in rpm results even though
there is normally about ¼ of the total travel still available. My throttle
body is a cut down Mazda one with two openings as described in Tracy’s
guide. Since I use the stock oil metering pump, the throttle position adjusts
the metering pump stroke and advancing the throttle more than necessary results
in accumulation of oil in the sump. At one point when checking the throttle
position, the RPM actually dropped slightly when advancing the throttle
further. I thought to myself “this is strange” and returned the
throttle to its original setting since things were running smoothly.
At the Rotorfest, I listened with interest
to Mark’s presentation on muffler lifetime or lack thereof, wondering why
my first attempt at a muffler had survived so long. I attributed this to my
normal operation at high density altitudes which results in reduced max power
levels. I also described the construction of my “bomb” to several people
who were interested in it. I now realize that I didn’t know what was in
it myself. During the preflight before leaving the Rotorfest, I noticed a
rattle in the muffler when checking its security to the belly of the plane.
After returning to Laramie, I investigated the rattle further and the results
are shown in the attached pictures. The fact that the center baffle broke is
not surprising since it was simply a push fit into the shell and was vulnerable
to flexing since it was flat. The repair uses a conical shaped baffle with a
solid ring around its outside circumference to make it even stiffer. We’ll
see how long that lasts.
The recent discussion on not developing
full power, especially Ed’s information on seeing almost 20 gph at max
power settings at seal level got me thinking about my performance. I have seen
up to 16 gal/hr at 4500 ft DA on a rare excursion to that low an altitude. That
didn’t seem unreasonable considering the sophistication of my setup
compared to Ed’s. Looking back at the data log from the flight home from
the Rotorfest, there were some interesting observations concerning the
departure from 40XS. That segment of some of the data from the log is shown in
the attached plots.
A couple of things in the data seem to me
to stand out. One is that I am recovering nearly full manifold pressure in the
plenum at wide open throttle compared to ambient as shown in the data of the
manifold pressure before start-up and during runup and take off. This has
always been the case. The second thing that stands out is that I was only
using between 10 and 11 gal/hr at wide open throttle with the mixture adjusted
for max power. I didn’t look at the fuel flow reading during runup or
take off and only noticed these low values when examining the data log
recently. I am confident that the fuel flow readings are quite accurate since
the fuel actually used for this trip matches the instrument readout very well.
While some of you may have experienced some apprehension at such a pathetic
power production level, it seemed normal to me since I usually operate at density
altitude from 7000-10000 ft. Another thing I noticed in the data is the significant
rpm drop when the prop unstalled just prior to liftoff. The rpm usually drops
a little at that point but not nearly this much. I remember noticing this on
departure, but was otherwise occupied and didn’t give much further
thought at the time. Not shown in the plots is the coolant temperature which
reached 225 degrees at the stock location in the flywheel end iron at 8 minutes
into the log. This is about 20 degrees higher than normal even at the reduced
fuel consumption level during this time. Oil temperature showed a similar
response.
After removing the muffler to investigate
the rattle, standing it on end would allow the broken segment to move to the
area of the outlet and block some of the exhaust exit area. Laying it
horizontally again would allow the broken segment to slide down the conical end
where it could not be seen in the exit. I suspect that the exhaust gas carried
the broken segment up the slope where it could block part of the exit when
operating at power levels above idle. Luckily, the blockage was not enough to prevent
generating enough power to sustain flight.
In any case, the data log is a record of
the effect of increased back pressure on the performance of my NA 13B. Just as
has been described in the recent discussions, the result was as expected:
decreased max fuel consumption and decreased max power production. In
addition, I saw increased coolant and oil temperatures. Maybe the increased
back pressure was responsible for the decrease in rpm upon fully opening the
throttle in stabilized flight, but I’m not sure why such an effect would
arise.
For what it is worth…
Steve Boese