Anybody know the torque spec for the 2 larger diameter
tension bolts (21mm head) that go in from the front on a 20B?
I discovered that there was a coolant leak into the oil, and
after removal of the engine from the plane in order to get the pan off; I discovered
the 21mm tension bolt inside the front cover had not been tightened. Then found
the other behind the CAS was also loose. Last year I had an external leak
at one of the 21mm bolts a the rear housing, and found that the two at the back
had not been torqued. Pretty hard to imagine a rebuilder overlooking torquing
the main bolts that hold an engine together.
Al