Friday, I went down to SC to replace my fuel rail, which had developed a
slight leak. Had three days of
perfect weather. High temperatures
in the upper 60’s, clear skies, and light winds. I replaced the fuel rail, and
after switching to different o-rings on the RC engineering injectors, I got a
perfect seal. The stock Mazda
seals would not work on these injectors, but thankfully Paul Brannon had the
correct o-rings.
It was getting dusk, but I managed to get in one trip around the
pattern.
On Saturday I made two flights, totally a little over an hour, and
everything ran great. Well, other
than I messed with the mixture on mode 3, and ended up being too lean when I
throttled down in the pattern.
Yesterday, I made the flight of about 190 NM and the plane and engine
were perfect. It was a beautiful
day, and while not unlimited visibility, it was probably 30-40 miles, clear
skies, and very smooth air at my cruising altitude of 3500 MSL. I flew the trip at about 55-60 % power,
since I am still nursing along my stock turbo. Still made about 125-130 KTS, and only took about 90 minutes
to make the trip, with a 10 KT headwind most of the way. It was very nice, after all the little
problems I had, to have a trouble free flight. The rotary engine just signs along, not missing a beat.
OAT was about 67 degrees, and engines temperatures ran at 185 on coolant
and 180 on the oil, at 4800 RPM’s.
The oil is a digital display that should be very accurate. The coolant is an analog gauge, so the
185 is more of a guess. The needle
was slight above the 180 mark.
I also got to see the first flight of Paul and Lou’s Lancair with the
20B. I’m sure that one of them
will tell everyone about it.
Steve Brooks
Cozy MKIV N75CZ
Turbo 13B – 47 hours