Just to let you know that flight testing is continuing,
and we’ve just passed 15 hours of flight time. Overall, the plane
and engine are doing fine. Things are trimmed out now for straight and
true handling. The
remaining issue is too much canard
lift, even after reducing incidence by a bit over 1 degree. It limits high speed end (run out of elevator
to keep it from climbing), and requires pretty hot landing (over the fence at
90 KIAS). The consensus of the experts is to shorten the canard (cut about 4”
sections out of both sides). Ouch!!
I am very pleased with the operation of the 3–rotor
rotary engine – in spite of few glitches still with the ECU, apparently some sort of electrical noise issue.
It starts easily hot or cold, runs smooth, plenty of power, and easy one-lever
operation. Haven’t established top end yet, but did get up to about 205
KTAS (175 KIAS at DA of close to 10,000 ft), and
there was still some to go. After gear up on takeoff the
VSI strip pegs out at 1000 fpm with close to 2100 # total weight. If you want
fast descent; gear down, power off (no worries about shock cooling), and push
both rudders out. Nice high controlled sink rate.
No good data yet on
fuel burn. I think it was calibrated fairly close, and read about 13 gph
at about 160 indicated, but then the EM2 suddenly started reading about half
that number, and I haven’t figured that out yet. Lots of work and testing left to
do.
Al