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Al, looks like your inlet is too flush with the surface. I'm with the impression that the boundry layer at the aft section of the plane could be up-to 1" thick. Since you'll be reworking this section anyway, I would form an temporary aluminum scoop extension and extend the lip to about 2" opening instead of 1/2". Just to see if you are moving in the right direction.
Looks like you don't have any ram pressure. My scoop is huge and ugly, but it feeds the oil cooler, radiator and ram air for the intake. It is about 1" lower than the bottom of the fuselage.
Bulent "Buly" Aliev
FXE Ft lauderdale, FL
http://tinyurl.com/s5xw8
CowlInlet.jpg
On Aug 6, 2006, at 9:45 PM, Al Gietzen wrote:
Thanks everyone for the congratulatory messages, and for the support that is always so helpful. No pics to post yet because my camera battery went dead after the first three shots, so I’m awaiting for shots from my friend who took hundreds (OK, only about 150) and will be editing for a while J.
The principal issue of the day was the higher than comfortable oil temperature; most likely due to insufficient air flow through the cooler. For anyone who would like to think aerodynamics for awhile and give an opinion on the simplest and best approach to remedy; read on.
The custom cooler for this 265 hp engine is large. The core here is about 5 ¼” wide, 22” long and 3 ¼” thick. It is located in the wing root of the Velocity, behind the spar, with inlet underneath and exit on the top. Alan Shaw, who I believe pioneered this approach, found the location worked very well. When I discussed the installation with him years ago, he opined that a scoop under the wing was probably not necessary because of a pressure differential between bottom and top surfaces. Since then, my investigations of pressure distributions, and similar installations that aren’t working so well, make me wonder.
Photo 1 is a view under the wing showing the OC air intake, wheel well, and the big armpit scoop for the coolant radiator in the cowl. The inlet opening is about 1 1/8” wide and 23” long. There really isn’t a scoop, just an opening with an extended airfoil shaped lip which extends about ½” into the free stream. The idea was to minimize drag, and assume a more negative pressure at the exit would produce the necessary flow. Photo 2 shows a front view where you see the wheel well and the inlet – very little extension into the free stream. Analysis suggests that the turbulent boundary layer on a smooth surface at the inlet location could be about 5/8 – 3/4” in thick.
The air exit fairing is shown in photo 3; and is shaped as it is to maintain attached flow and cause minimal turbulence going aft. The effective exit area is about 1.6 times the inlet area. The thickness of the core suggests the need for pretty good pressure differential for adequate flow.
Here are some options:
a) For the first flight the landing gear was never retracted. Since the open wheel well forward of the inlet would likely cause significant turbulence; try another flight with the gear retracted to see if that improves the results.
b) Place some VGs forward of the inlet to ‘energize’ the boundary layer, and see if that helps.
c) Extend the ‘lip’ of the inlet to form a proper ram scoop, possible also with VGs forward to break up the boundary layer, and accept the slight increase in drag.
d) Do something at the exit ( local ‘expert’ suggests there may be flow separation before the aft end of the fairing causing high pressure behind the exit). Put VGs on the top of the exit fairing and/or reduce exit area.
e) None of the above.
I suspect the normal aerodynamic pressure differential between the inlet and outlet points is minimal; especially in level flight where it could be near zero. Option c) seems the most sure-fire to me.
Thanks for input.
Al
<OC inlet 1.JPG>
<OC inlet 2.JPG>
<OC outlet 1.JPG>
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