Hi, Marc....I would absoulutely LOVE to have that
tape !!!! Please mail or UPS it to me, and I will of course send you the
money for shipping right away. Thanks so much for taking the time to do
this. Paul Conner, 5181 Southern Oaks Trail, Grand Bay, AL
36541
----- Original Message -----
Sent: Tuesday, August 17, 2004 7:20
AM
Subject: [FlyRotary] Re: First flight
test report on Renesis
Paul, You're building an SQ2000, right?
I looked at that kit a number of years ago, but they went out of business just
before I was ready to send them a check. Anyway, I had ordered their
information packet with demo tape. I still have the tape, so if you want
it for your library, its yours. I could bring it to Tracy's fly-in if
you're planning on attending, or I could just mail it.
Mark S.
At 07:57 PM 8/16/2004 -0500, you wrote:
Hi,
Tracy.....thanks so much for taking the time to write such a detailed
description of the first Renesis flight. We all appreciate your
efforts, and especially your efforts to share your results. Best of
luck in bringing down the temperatures. Paul Conner, 13b powered
SQ2000 canard
- ----- Original Message -----
- From: Tracy Crook
- To: Rotary motors in
aircraft
- Sent: Monday, August 16, 2004 2:38 PM
- Subject: [FlyRotary] First flight test report on Renesis
- The first test created more questions than answers and much work to
do. Here is my development log entry for the flight.
- Tracy
- (8-15-04)
- Flight test report on Renesis engine installation, N84TC
- OAT 88 90 deg
- Humidity 90+%
- Pilot impressions:
- Takeoff done with engine warm (~ 155 F) but water Temp was 207
on first check after rotation. Reduced throttle and orbited SB for
64 minutes at ~ 1000 ft. MSL. Engine very smooth with low cockpit
noise level. Water temp slowly fell to 195 197 at fuel burn of 5
5.5 GPH. Engine RPM was 4300 4700 during flight. Very brief
(few seconds) full throttle test yielded only 5800 rpm and engine did not
feel strong. MAP appeared to be limited to ~ 28 Hg. Water temp
immediately climbed to ~ 205 and power was reduced. Oil pressure
continued to read 100 PSI (full scale on instrument) as it has during
ground tests. Engine builder used 3rd gen rear pressure
regulator and it has been my assumption that this was normal for it. Reset
oil pressure high limit on engine monitor to 102 PSI to get rid of
flashing alarm. Oil temps were stable at 185F during entire
flight. Normal landing with engine temps falling rapidly during
final approach.
- Post flight engine check (engine still hot):
- Gear drive had normal system lash
- Turning over engine w/ prop, engine felt tight, higher friction than
previous checks.
- Rotor compression felt normal (very good) but feel was hampered by
engine friction.
- Smell test through cooling inlets: Aroma was very different than
earlier engine installation although no sign of anything bad.
- Significant data:
- Air temp delta on right side rad was 80 85 deg F
- Water temp delta: 20 25 F
- Oil temp delta: ~ 30 F
- Oil cooler air temp delta was ~ 45 - 50 F which was normal at the low
power setting being tested.
- MAP at WOT appeared to be 1.5 2.0 below atmospheric.
- Analysis: High coolant temperature was very disappointing as I
had expected much better cooling with the improved diffusers.
Reasons for the high temps can be surmised by delta temps above. The
high air temp Delta would indicate one of two things:
- 1. higher coolant temps indicating more heat rejection,
or
- 2. Lower airflow through rad.
- The coolant temp was higher but only marginally (10 deg after
stabilized at 195) This would not account for a 30+ deg increase in
air delta. This leads me to believe that reduced airflow is the
cause. The diffuser on this rad cannot possibly (?) be worse
than before so my guess is that the greatly extended duct divider that
separates the oil cooler duct from the rad duct is having an adverse
effect. Oil cooling was not a problem and delta was in normal range
so it was not hurt by the divider and may even have been improved.
- The water temp delta would indicate that the water flow rate is less
than half of the previous value when deltas were in the range of 10 12
F. Two possible causes come to mind.
- 1. The coolant manifolds I made are too restrictive.
- 2. The water pump design is less effective than the 2nd
gen engine.
- 1 was a concern even while I was building them. I thought they
would be adequate because the coolant outlet arrangement does not appear
to be any more restrictive than the previous setup. OTOH, the
inlet setup could be significantly worse than before. It has 90
degree fittings which could be a problem.
- The water pump design is the same as the 3rd gen 13B which looks
crude by comparison to the 2nd gen but has evidently been adequate
in the auto racing environment. It may require a much cleaner
coolant path in order to achieve adequate circulation. Or
conversely, the 2nd gen pump may be much more tolerant of
restrictive coolant paths.
- Oil Pressure
- The 100 (+?) psi oil pressure is a concern after learning from the
engine builder that the 3rd gen oil pressure regulator (presumably
equipped with a Renesis regulator spring) is supposed to give
pressure in the range of 70 85 psi. This would indicate that the
pressure is being regulated not by the rear regulator but the front
pressure relief regulator which does not become active until 150+
psi. As I write this, I decided to check the Racing Beat
Tech manual for info on oil pressure. According to their chart, the
93 -95 rear pressure regulator is set at 110 PSI !. This leaves me
with no firm conclusion about the oil pressure readings.
- Engine builder later confirmed that he had pressure spec wrong.
3rd gen is specified as 110 psi. A 3rd gen car racer
also said that his oil pressure runs 85 95 psi hot. Off scale when
cold. Have canceled tentative plans to pull the engine for this
problem. I would still prefer to have a lower pressure regulator and
will do this if I have another opportunity.
- Low MAP
- This problem is probably due to the relatively long and tortuous path
between the NACA inlet and throttle body. There is over 4 feet of
2.75 Dia. Aeroduct (SCEET?) between the two. I was concerned from
the start that this stuff would cause a pressure drop. It will have
to go. Many more hours of fiberglass work required to fix.
- Did prop pull-through test of engine feel and it was same as earlier
tests prior to flight test. Compression of engine when pulled
through in reverse is impressive.
- Confirmed that the air temp sensor behind right rad was
accurate. In view of this I have decided to cut the duct divider
back to near its original position and re-test.
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